Equipment/Makerbot Cupcake: Difference between revisions

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==Logbook==
==Logbook==
===11/02/2010 operator; Glen===
* To print warp free large objects heat the perspex plastic bed to 100'C with the hot air blower then make sure the first two base layers are stuck to the bed by adjusting the Z-axis height. Don't use the electric fan heater as this increases cooling of the plastic. I used the hot air de-soldering blower at 100'C to keep the plastic warm while printing, though I didn't try printing without this.
* The extruder gear wheel has a part missing from it that limits where the plastic feed can rest against the gear teeth. Until the drive gear is replaced the plastic feed can work it's way next to the idler wheel where it will no longer be driven. I tried putting two idler wheels in to stop the feed from having any space to get away from the drive gear, but this didn't work so I went home.
* Consider selling the printer to some poor fool on eBay, as far as I know it's printed no large objects despite receiving dozens of hours of maintenance and is clearly possessed by angry spirits.


===09/02/2010 Operator: Russ===
===09/02/2010 Operator: Russ===

Revision as of 11:33, 11 February 2010

We have a Makerbot Cupcake (batch 9, #402)! It's cool.

If you haven't used it before, please contact Russ and get him to show you how it works.

If you're using the Makerbot and have issues with it, or have to do maintenance/modifications to it, please note them in the logbook below. This lets other users know what the state of the machine is.

Logbook

11/02/2010 operator; Glen

  • To print warp free large objects heat the perspex plastic bed to 100'C with the hot air blower then make sure the first two base layers are stuck to the bed by adjusting the Z-axis height. Don't use the electric fan heater as this increases cooling of the plastic. I used the hot air de-soldering blower at 100'C to keep the plastic warm while printing, though I didn't try printing without this.
  • The extruder gear wheel has a part missing from it that limits where the plastic feed can rest against the gear teeth. Until the drive gear is replaced the plastic feed can work it's way next to the idler wheel where it will no longer be driven. I tried putting two idler wheels in to stop the feed from having any space to get away from the drive gear, but this didn't work so I went home.
  • Consider selling the printer to some poor fool on eBay, as far as I know it's printed no large objects despite receiving dozens of hours of maintenance and is clearly possessed by angry spirits.

09/02/2010 Operator: Russ

  • Extruder with 2 idler wheels doesn't appear to work at all.
  • Reassembled the extruder with one idler wheel, moving the drive wheel up the shaft a little.
  • This works, but the extruder stalls after a random amount of time! WTF. We need a new drive wheel.

08/02/2010 Operator: Glen

  • Can printed half a large object with no warping by melting the raft to the print surface.
  • Print-head failed push plastic feed into nozzle
  • Dismantled the print-head and found the gear that drives the plastic feed stock had broken in two and the two parts had ground against each other to produce many tiny metal shards.
  • After cleaning the print-head the plastic would not come through unless pushed by hand.

06/02/2010 Operator: Russ

  • Downgraded both motherboard and extruder to 1.5 firmware.
  • Printing off SD card, no crashes observed.
  • Managed to get about 80% of a shot glass printed. Glitches caused by contraction were an issue, and eventually it got knocked off by the print head.
  • I'm fairly sure the hardware is working fine. Problems I'm now seeing are caused by either ambient temperature/airflow or skeinforge settings.

04/02/2010 Operator: Russ

  • Walked in, started it up, extruder works fine.
  • Extruder idler pulley needed re-adjusting twice. (Note: that the thin silvery metal bar in the Makerbot toolkit is designed to be used as a spacer for this.) Should be done up nice and tight now though.
  • Continual tweaking of z-stage stepper strength, now at about 75%
  • Accidental Z-stage/build platform collision required re-levelling of Z-stage (seems the best way to do this is by releasing one of the Z idler pulleys and twisting the studding, instead of fiddling with the nuts). Seems pretty smooth now.
  • X belt tension was too low, there was a lot of slop. It's pretty tricky to get it tight enough.
  • Lots of bolts on the XY stage were loose! This makes a horrendous racket when it's actually printing at full speed... Tightened them up
  • Packed both X runner bars with hot glue, they were also moving about and making a racket.
  • I managed to make it print 1/3rd of a shot glass, then it crashed. (About 60,000 gcode commands/30mins in.) Need to know what firmware to put on it to stop the crashing.

Following changes over skeinforge 0006 defaults are active (on my laptop):

 Feedrate: 27.0 mm/s
 Base Layer Thickness over Layer Thickness:  1.5
 Interface Layer Thickness over Layer Thickness: 0.8