Difference between revisions of "Project:Blood typing"

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'''Conclusions:'''
 
'''Conclusions:'''
  
This needs to be repeated to confirm, but it seems to show that the ethanol precipitated DNA worked in PCR, even though it looked like none had dissolved, while the chelex didn't. If at least one has worked that's good news. It's strange though that the chelex extraction shows up as genomic in the well, but failed PCR, whereas the ethanol extraction is the other way round. Possible that something in chelex mix inhibited PCR, while quantity of genomic was too little to show up for ethanol, but was enough for PCR. nb. Chelex PCR product was oddly small compared to other.
+
This needs to be repeated to confirm, but it seems to show that the ethanol precipitated DNA worked in PCR, even though it looked like none had dissolved, while the chelex didn't. If at least one has worked that's good news. It's strange though that the chelex extraction shows up as genomic in the well, but failed PCR, whereas the ethanol extraction is the other way round. Possible that something in chelex mix inhibited PCR, while quantity of genomic was too little to show up for ethanol, but was enough for PCR. Possibility of mix up in pipetting.
  
 
Mailing list discussion [https://groups.google.com/forum/?fromgroups=#!topic/london-biohackers/1bfCry6ryEc here]
 
Mailing list discussion [https://groups.google.com/forum/?fromgroups=#!topic/london-biohackers/1bfCry6ryEc here]

Revision as of 13:39, 8 November 2012

How genes code for blood group

Blood group is determined by the combination of A and B antigens in your red blood cells. A and B individuals have only their respective corresponding antigens, AB individuals have both, and O individuals have none.

The production of these antigens is determined by the "histo-blood group ABO system transferase" gene (1062 base pairs), which is part of the ABO gene locus. This gene codes for the expression of a glycosyltransferase enzyme which by acting on another antigen(H), produces A or B antigens. The A and B allelic forms of the gene code for different forms of glycosyltransferase which affect the H antigen in different ways. O alleles code for another protein that doesn't affect the H antigen, meaning no A or B antigens are expressed. O alleles have a deletion of G at 258, while B alleles have a single nucleotide polymorphism (SNP) from G to A at position 700. The gene we're looking at is here: ABO gene. You need to set the origin to 29 under the tools menu, as this viewer is for the entire ABO gene; the histo-blood group ABO system transferase gene doesn't start until position 29.

Each person has two of these alleles, one from each parent. A and B are dominant, O is recessive, so the possible combinations are:

Alleles Blood group
AA A
AO A
BB B
BO B
AB AB
OO O

In the UK the distribution of A, B, AB and O is 42%, 10%, 4% and 44%.

Process overview

1) Obtain two sequences of DNA through PCR, the first containing the deletion site at 258, and the second containing the SNP site at 700

2) Use restriction enzyme KpnI on the first fragment to cut the O alleles only, and use restriction enzyme AluI on the second fragment to cut the B alleles only. (KpnI's cutting site is GGTAC^C - this sequence is found in 0 alleles, but in A and B alleles the sequence is GGTGACC, hence they are not cut. AluI's cutting site is AG^CT - in A and O alleles the initial A is a G, hence only B alleles are cut.)

3) Do gel electrophoresis on the resulting fragments, hopefully resulting in distinguishable bands to show the 6 different alleles. We should then be able to determine an individual's blood type.

Process reality

Much of the necessary equipment we already have from the sex typing experiments. Of the new things, we need the restriction enzymes, and possible a new gel - see below.

All fragments in the papers are between 80 and 200 bp long. For this we would need a polyacrylamide gel (which we have decided against due to difficulty with handling) or a high quality agarose concentrated at 3%, which is a bit expensive, but not impossible. So we have decided to design our own primers to get larger fragments to work with.

Design of primers for larger fragments:

Using the ApE software, we have found a set of primers to enable us to use longer fragments. Here is the file with the primer sequences (Save this link as a file): ApE file, and Download ApE here

Primers for G deletion sequence:

Primer Sequence Length GC% Tm(°C)
P1 forward 17484 5' CCCGCAGGTCCAATGTTGAG 3' 17503 20 60 59
P1 reverse 18268 5' ATCTGACAGAGAAGTGACCACG 3' 18247 22 50 58

Product is 784bp.

After digestion with KpnI you get two sizes of fragments - 243bp and 541bp


Primers for G to A SNP:

Primer Sequence Length GC% Tm(°C)
P2 forward 19125 5' GAGGTGGATTACCTGGTGTGC 3' 19145 21 57 59
P2 reverse 19473 5' GCACCTTGGTGGGTTTGTGG 3' 19454 20 60 60

Product: 347 bp.

After digestion with AluI : two fragment sizes of 96 bp and 251 bp

New equipment

Sigma aldrich have KpnI and AluI. I couldn't find them on NBS bio. A cheaper alternative is to try to get them from NEB (http://www.neb.uk.com/).

If we do need high quality agarose here is sigma's selection. NBSbio have agarose but no info on its purity.

Sources

Most of the procedure came from this paper. With some more here. For other papers and background see here.

Here is a sequence viewer for the ABO gene. Histo-blood group ABO system transferase starts at position 28 - so to find the deletion at 258 and the SNP at 700 you have to add 28 to the numbers on the viewer. Go from the 5' end.

Extraction and PCR 15/8

  • Extract DNA (two samples, Will and Nicholas) from cheek by rubbing with pipette tip and taking saliva
  • Mix with 250ul of chelex 100, cover with a drop of oil and incubate at 56°C for 30 mins.
  • Centrifuge for 5 mins and remove supernatant. Supernatant kept to view genomic DNA later.
  • Two reactions prepared - Nicolas (AMELX/Y primers), Will (PB1 primers)
  • Reaction volume - 12.5ul Taq, 5ul template, 5ul primers, 2.5ul deionised water.
  • PCR: initial denaturation at 96°C for 5 mins, then 35 cycles of 96°C for 1 min, annealing at 55° for 30 secs, extension at 72°C for 1 min.
  • Results. PCR failed. Will's DNA was the one using blood typing primers.

Extraction and electrophoresis of genomic DNA 15-17/8

  • Add cheek scraping + saliva to 1/2 a PCR tube of chelex (half bead layer, half liquid layer). Mix
  • Incubate at 56°C for 30 mins, vortex briefly, 94°C for 10 mins. (Should have centrifuged and) take supernatant.
  • Add 5ul of loading buffer to 25ul of template - visualise on 1% agarose gel
  • DNA visible in well.

Extraction and PCR 19-20/8/12 (Will)

  • Chelex extraction. Visualised and saw glow in well so proceeded to use this as template.
  • 25ul total reaction volumes. Quantities assumed as no record: 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC).
  • Initial D - 96C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
Gel run 20th Oct

From right:

  • 1: 250-10000bp ladder (from hackspace). Ladder key
  • 2: PC + amelogenin (sex typing) primers (combined aliquot)
  • 3: PC + amelogenin (sex typing) primers (separate aliquots)
  • 4: PC + PB1 primers
  • 5: Template put through PCR program with no other reagents
  • 6: Template + separate AMEL primers
  • 7: Template + separate PB1 primers
  • 8: Template - no PCR

Conclusions:

  • As PC worked with PB1 primers but not AMEL, there is either a problem with the AMEL primers, or the annealing temperature of 55C doesn't work for them.
  • Something in the reagents / template stops PCR working for our extractions OR there is too little DNA extracted. However even if the extracted DNA is very little, surely is enough for PCR? And we are pretty sure there is DNA there because it shows up genomically in the wells.

discussion


Extraction and PCR 03/10

  • About 2ul of saliva scraped from cheek + 325ul chelex (half bead layer, half liquid layer). Mix.
  • Incubate at 56°C for 30 mins (missed vortex), 94°C for 10 mins. Centrifuge and take supernatant.
  • PCR mix: 5ul template, 5ul primers, 2.5ul dH20, 12.5ul Jumpstart taq readymix
  • Positive control: 1ul template, 5ul primers, 6.5ul dH20, 12.5ul Jumpstart taq readymix
  • PCR: 94C 2min, 30 cycles (94C 30s, 56C 30s, 72C 2min), 72C 5min.
Gel run 3rd Oct

From left:

  • 1: 250-10000bp ladder (from hackspace). Ladder key
  • 2: Positive control PCR product.
  • 3: Mike PCR product
  • 4: Simon PCR product
  • 5: Will PCR product
  • 6: MF1 (From UCL)
  • 7: N.H / N.1+ (From UCL)

The positive control worked (You can see if you look closely). However the band was significantly weaker than the gel run on August 20th with same PC + same primers. None of the PCRs on our extractions worked.

I also ran our 3 genomic samples, and nothing was there - providing a reason for PCR failure.


Extraction 25/10 (Done by Will and Lui)

  • 10ml dH20 vigorously rinsed in mouth (with cheek biting) for 3 mins
  • Spat out, added ∼1.5ml washing up liquid, mixed, left for ∼10 mins.
  • Split samples into two groups

1st group:

  • Took ∼500ul sample, added ∼100ul Proteinase K solution
  • Incubated for 1hr at 50C, 10 mins 94C
  • Added 1 volume 100% EtOh, small amount of precipitate observed, so centrifuged at 13000 rpm for 20 mins
  • Dried at ∼50C
  • Added ∼350ul 70% IPA, centrifuged at 13000 rpm for 10 mins
  • Air dried pellet
  • Tried to resuspend in 500ul TE but pellet wouldn't resuspend completely. Unsure if none had dissolved or some had. Even incubating at 60C didn't work. Edit - seemed none dissolved as nothing showed up on gel. Didn't dissolve even in 10 ml dH20.

2nd group (remainder of sample - 11ml:

  • Added 10 shakes meat tenderiser
  • Added 1/2 volume 70% IPA. Significant amount of precipitate observed. Able to remove it with pipette.
  • Dried at ∼50C
  • Split, washed one with 70% IPA, centrifuged 10min at 13000 RPM. Then resuspended pellet in 500ul TE. Other only resuspended, no wash. Resuspensions didn't totally work (not sure if any dissolved).

PCR of 1st group 27/10 (Will's sample)

  • 25ul total volume - 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC)
  • PCR was Initial D - 95C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
  • Gel - loaded 5ul of ladder, 15ul of each sample, ∼ 0.2 vol loading buffer
Gel run 27 Oct

From right (after 35 mins at ∼ 80V:)

  • 1: 250-10000bp ladder. Ladder key (At the far right, you can barely see it)
  • 2: Will PCR product (PB1 primers) (Nothing)
  • 3: Positive control PCR product (PB1 primers) - We expect this to be 784 bp, looks right.
  • 4: Positive control PCR product (PB2 primers) - We expect this to be 347 bp, looks right.
  • 5: Will genomic (Nothing)

Conclusions:

  • Something went wrong with the ladder - it's barely visible. I used standard quantity so unsure why.
  • My extractions failed PCR, and nothing showed up in genomic - hence extractions failed. If the pellet was DNA and had not degraded, it just must not have dissolved.
  • Both controls worked - so both sets of our blood typing primers work.


Extraction 28/10

  • Used this protocol. No DNA precipitated, so resolved to try again tomorrow using cheek swish method instead of cheek scrape.

Extraction 29/10

  • Used this protocol. Instead of scraping cells from cheek, swished 5ml of dH20 in mouth for 3 mins while chewing cheeks. Then took 200ul of this and proceeded with extraction.
  1. One reaction had 1% Triton. 150ul of sample + lysis buffer added to 50ul PK. Incubated. No precipitate observed, but washed where pellet would be with 70% Etoh. Stored in freezer in 70% Etoh.
  2. One reaction had 10% Triton. 150ul of sample + lysis buffer added to 50ul PK. Incubated. No precipitate observed, but washed where pellet would be with 70% Etoh. Stored in freezer in 70% Etoh.
  3. Added 0.5ml dishwashing detergent to 'mouth swish remainder' (4.5ml). Added a few shakes meat tenderiser. Took ∼150ul, centrifuged and took supernatant. Added 0.25 vol PK and incubated. Precipitated and washed, small amount of DNA observed, tried to resuspend but wouldn't dissolve. Stored at -20C.
  4. Used IPA to precipitate the rest. Large pellet extracted, air dryed for 5 mins, then would not dissolve in 300ul TE at 65C. Stored at -20C.

Extraction and PCR 31/10 (Will)

  • Extracted DNA from cheek using this protocol
  • Ran PCR with PB2 primers on this sample + the third sample from the 29/10 + a positive control.
  • 25ul total volume - 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC)
  • Initial D - 95C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
Gel run 31 Oct

From left (after ∼40 mins at 80V:)

  • 1: 250-10000bp ladder. Ladder key
  • 2: Will PCR product (Chelex extraction) (Nothing there)
  • 3: Will PCR product (Ethanol extraction) - We expect this to be 347 bp, looks right.
  • 4: Positive control PCR product - We expect this to be 347 bp, looks right.
  • 5: Chelex extraction genomic
  • 6: Ethanol extraction genomic (Nothing there)

Conclusions:

This needs to be repeated to confirm, but it seems to show that the ethanol precipitated DNA worked in PCR, even though it looked like none had dissolved, while the chelex didn't. If at least one has worked that's good news. It's strange though that the chelex extraction shows up as genomic in the well, but failed PCR, whereas the ethanol extraction is the other way round. Possible that something in chelex mix inhibited PCR, while quantity of genomic was too little to show up for ethanol, but was enough for PCR. Possibility of mix up in pipetting.

Mailing list discussion here


PCR 1st Nov 2012 (Will)

Repeated PCR from 31 Oct to test conclusions.

  • Same inputs except that the chelex solution was centrifuged and resulting pellet discarded before PCR. Also another sample from 29/10 used in addition to one from last time. PB2 primers used.
  • 25ul intended total volume - 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC). Actually put 6.5ul of dH20 in each sample by mistake, meaning total volume of 29ul for all except PC.
  • Initial D - 95C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
Gel run 1 Nov

From left (after 40 mins at 80V:)

  • 1: 250-10000bp ladder. Ladder key
  • 2: Will PCR product (Chelex extraction) - We expect this to be 347 bp.
  • 3: Will PCR product (3rd Ethanol extraction from 29/10) - Nothing
  • 4: Will PCR product (1st Ethanol extraction from 29/10) - Nothing
  • 5: Positive control PCR product - We expect this to be 347 bp
  • 6: Chelex extraction genomic

Lanes 7 and 8 not visible on photo

  • 7: 3rd Ethanol extraction genomic (Nothing there)
  • 8: 1st Ethanol extraction genomic (Nothing there)

Conclusions:

Most likely this means that I mixed up chelex and ethanol extractions for the run on the previous day, and chelex actually worked then too. Less likely is that chelex worked this time but not last time, either because I removed PCR inhibitors with the centrifuge, or because we avoided the problem of small reaction volume discussed previously. This would also mean that the ethanol precipitated sample has stopped working. Need to do more to confirm. Odd that chelex genomic showed such a strong band last time but none this time.

Mailing list discussion here


Extraction and PCR 04/11 (Will)

  • Extracted DNA from cheek using this protocol. Pellet quantity was larger than previous time, as swished in mouth for 1 min. perhaps too large.
  • Ran PCR with PB2 primers on new chelex extraction from 4/11 + old chelex extraction from 31/10 + third sample from the 29/10 + a positive control.
  • 25ul total PCR reaction volume - 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC)
  • Initial D - 96C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
Gel run 4 Nov

From left (after 40 mins at 80V:)

  • 1: 250-10000bp ladder. Ladder key
  • 2: Will PCR product (4/11 Chelex extraction) - Nothing there
  • 3: Will PCR product (31/10 Chelex extraction) - Good band
  • 4: Will PCR product (3rd Ethanol extraction from 29/10) - Weak band
  • 5: Positive control PCR product - No band
  • 6: Chelex extraction 4/11 genomic - band

Lanes 7 and 8 not visible on photo

  • 7: Chelex extraction 31/10 (Nothing there)
  • 8: 3rd Ethanol extraction 29/10 genomic (Nothing there)


Conclusion:

This time the new chelex extraction didn't work (but showed up as gDNA. Will want to try again, possibly used too much. 31/10 chelex worked as expected. Old ethanol worked too, which was a surprise. Positive control didn't work, seemed very small volume after PCR, possible reason.

Extraction and PCR 07/11 (Will, Nicholas, Adam, Jim)

  • Nick, Adam and Jim extracted DNA from their cheeks using this protocol.
  • Ran PCR with PB2 primers on these 3 + Will's chelex extraction from 4/11 + Will's chelex extraction from 31/10 + Will's third sample from the 29/10 + a positive control.
  • 25ul total PCR reaction volume - 5ul template (1ul for PC), 5ul primers, 12.5ul Taq readymix, 2.5ul dH20 (6.5ul for PC)
  • Initial D - 96C 5 mins, then 35 cycles of D-96C 1 min, A-55C 30 secs, E-72C 1 min.
Gel 8 Nov

From left (after 40 mins at 80V:)

  • 1: 250-10000bp ladder. Ladder key
  • 2: Nick PCR product
  • 3: Adam PCR product
  • 4: Jim PCR product
  • 5: PC PCR product - nothing (low volume after PCR. Perhaps evaporation)
  • 6: Will PCR product (4/11 Chelex extraction) - nothing
  • 7: Will PCR product (31/10 Chelex extraction) - nothing (low volume after PCR. Perhaps evaporation)
  • 8: Will PCR product (29/10 3rd Ethanol precipitation)
  • 9: Nick gDNA - small amount visible in well (but not in photo)

Lanes 10, 11 and 12 not in photo

  • 10: Adam gDNA - visible in well
  • 11: Jim gDNA - not visible in well
  • 12: Will gDNA (4/11 chelex extraction) - small amount visible in well + smear running ahead of ladder (disappeared over time)


Conclusions:

  • 2/3 of new chelex extractions worked, this is good. However they are very inconsistent despite using the same extraction protocol; Nick's is strong, Adam's faint, Jim's failed. Not sure why this is.
  • The ethanol precipitation extraction from 29/10 continued to work. This means we can try to get more successes with ethanol.
  • The two older chelex extractions didn't work. The 4/11 was expected to fail, as it failed last time. The 31/10 worked last time. Possible reason for failure this time was that volume was low coming out of PCR, with droplets on the side of the tube.
  • Positive control failed again. This also had low reaction volume coming out of PCR like last time, and droplets on the side of the tube, meaning evaporation is a possible reason.
  • Many samples had smears running ahead of them (these had gone by the time the photo was taken), which has not happened the last few times. This could be because this PCR was left overnight at 4C before the gel was run the next morning, leaving time for the DNA to degrade, whereas the last few gels were run straight away. Or (less likely) because unlike the last few times, autoclaved pipette tips were not used for the initial extractions.