Project:UMI RTX Robot arm

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Revision as of 21:19, 16 September 2012 by Mentar (talk | contribs)
UMI robot arm feeling poorly

6 DOF robot arm from 1986, Possibly being donated by Daithi.

Proposals

Mentar: I'd love to make a ROS package and an URDF model for the arm. I've compiled ROS on the Pi so can use that to get make a network node pretty easily. Would need to sort out the electronics on the arm. Personally it would be easier for me to just salvage the power electronics and replace with a Pi. But if someone wants to restore the stock electronics then I think you should have a bash first!

Updates

Update 11/09/2012

artag, jasperw and mentar took the arm apart to figure out the problem with the z-axis. Turns out it's not that bad, turns fine. The z-axis motor (24V) wasn't working because of the corrosion layer on the commutator, cleaning the brushes and rotating the motor axle cleaned off some of the corrosion and it works beautifully at 24v

Update 29/08/2012

Tomw and tgreer tried to get this running but the z axis seems to be rusted to f***. The PSU outputs the correct voltages but when trying to put this into "green mode" it buzzes and sticks in red.

Checked fuses and theyre ok.

We forced the z-axis to try and break it out of any rusted stickiness and managed to move it down. We also tried 12-24v across the z axis motor and got no response

One of the fuses then blew which we replaced and promptly blew the 5 tantalum capacitors near the right hand connector on the main board. These will need replacing

note: (artag) tantalum capacitors of this age have a tendency to die by going short-circuit. If the fuse allows it, they will then burn up fairly vigorously. Depnding on which ones died, you might be able to ignore this (once they've burnt open-circuit) but it would be best to replace the lot. There are about 4 1uF 35V, about 8 10uF 35V, and 1 47uF 35V.

Docs