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Project:UMI RTX Robot arm: Difference between revisions

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==== Update 28/05/2013 ====
==== Update 28/05/2013 ====


[[User:Mentar|Mentar]]: Fixed the elbow joint, hat to drill a jammed screw off. Traced out about half of the wires from the blue cable.
[[User:Mentar|Mentar]]: Fixed the elbow joint, had to drill a jammed screw off. Traced out about half of the wires from the blue cable, which control all the rotary joints


==== Update 16/03/2013 ====
==== Update 16/03/2013 ====